|
Can-Less
(A computer speaker; redux. December-2005)
Can-Can
(A computer speaker in a light canister. Jan-2005)
Shiva_PR15
(A powered subwoofer using a 12" driver and 15" passive
radiator. Work in progress. Aug-2003)
Sonosub
(10" vented subwoofer in a cardboard tube, powered by a Parapix
amp. May-1999)
MTM
Center Channel Speaker
(A Madisound design. Nov-1997)
2-way
Surround Speakers
(5" woofer and 1" tweeter. July 1997)
3-piece
mini system
(6" DVC bass module mated to 4" car speaker. June 1997)
3-way
Vented Floorstanding Speaker
(vented 10" woofer, 5" mid and 1" tweeter in a 4
ft tower. Summer 1995)
NHT1259
Subwoofer
(A 12" woofer in a sealed architectural pedestal. Winter 1994-95)
Inexpensive
Speaker Stands
(Particle board, sand and spray paint. Fall 1994)
2-way
satellite
(6.5" woofer and 1" tweeter. Summer/Fall 1994)
| Electronics
Related Projects |
A
PC-based Audio Console
(Use a PC to play tunes. Work in Progress. Feb-2004)
LM-12 Amp
(Bridged LM-12 opamps. Aug-2003)
CeeDeePee
(A CD player and FM tuner from spare computer parts. Oct-2002)
Quad
2000 4-Channel Amp
(Premade modules by Marantz. May-1998)
Zen
Amp and Bride of Zen Preamp
(by Nelson Pass. Apr-1997)
Backing-up
LPs to CD-R
(Whiningdog.net 10-Dec-2002)
Using Wood in Speakers FAQ
(Work in progress)
MDF
FAQ for speaker builders
Woodworking
Tools for the DYIer
(HomeTheaterHiFi.com Oct-1998)
Some Thoughts on Cabinet Finished for DIY
Speakers
Large
Grills Made Easy
Some
Parts Suppliers
(Outdated)
DIY
Audio Related URLs
Veneering Primer
(by Keith Lahteine)
How
to get a Black Piano Finish
(by DYI Loudspeaker List members)
Sonotube
FAQ
(by Gordon McGill)
Excerpts
from the Bass List
(Oldies but Goodies)
Current
DIY Loudspeaker Forum Home
Former
DIY Loudspeaker List Subscription Page
DIY
Loudspeaker List Archives
|
|
Sonosub
- An Inexpensive Powered Subwoofer (page 4)
Building
the Speaker (continued)
- At this
point, I evaluated the appearance of the endcaps. The top
was furniture grade plywood, but I wanted a cherry look
to better contrast with the granite green finish of the
tube. The veneer was birch, and when I applied a cherry
stain, it looked horrible. So I decided to add another layer
of cherry veneer plywood I already had.
- Glue
3/8 inch thick cherry veneered plywood to the top endcap.
Use a router with a pattern following bit to cut the
plywood flush with the existing endcap.
- For
the exposed edges, apply cherry edge banding to both
endcaps. This is an iron-on strip of real wood veneer
with pre-applied, heat activated glue.
- Applied
Watco Danish oil to cherry surfaces. Topcoat with a
thin layer of wax.
- Final
assembly.
- Glue
the plastic port tube to the bottom endcap/baffle using
RooClear plastic glue.
- Attach
two wires from the inside of the terminal cup. Solder
connectors to the driver ends of the wires to allow
easy connect/disconnect to/from the driver.
- Mount
the rectangular terminal cup to bottom endcap/baffle
with four screws. Use a small amount of rope caulk to
give it a good seat in the hole.
- Connect
the endcaps to the tube. On the first pass, I used rope
caulk to seal the endcap/tube interface. Later I glued
the tube to the endcaps making it effectively impossible
to disassemble the unit without destroying something.
Add a flat washer, lock washer and tighten the nuts
on the rods.
- Feet
- To
raise the unit off the ground (after all, this is a
downward firing sub) I made feet out of 4 hardwood balls.
These have a flat part and are sold as doll heads in
craft stores (they may also be sold for other purposes).
The ones I used are 3 inches in diameter.
[four
wooden "doll's heads" craft balls; 5,022 bytes]
- To
mount the flat part of the ball to the baffle, I made
a drilling jig. I drilled a 3/8 inch diameter hole through
a block of scrap wood to make the jig. The purpose of
the jig is to guide a drill bit perpendicularly into
the ball.
- Locate
the center of each ball's flat area. Position the hole
of the jig over the center of each foot and using the
jig as a drilling guide, drill a 3/8 inch diameter hole
about 1-1/2 inch deep hole into each ball.
- Cut
four lengths of 3/8 inch threaded rod from stock left-over
from the main conneting rods. These should be long enough
to go from the balls, through the baffle, and stick
out the other side with clearance for a flat washer,
lock washer and nut assembly.
[hardware
for each foot, plus jig block; 6,764 bytes]
- Epoxy
a piece of 3/8 inch threaded rod into each ball.
- To
locate the four feet accurately on the baffle, I made
another jig. This was 2 pieces of wood, half-lapped
onto one-another at right angle (makes a large '+' sign).
I marked off the radius from the center of the jig and
moved the jig about the baffle until all four sides
were equi-distant from the center based on the markings.
- Drill
3/8 inch diameter holes through the baffle for the feet
- Mount
and secure the feet with a flat washer, lock washer
and nut on the inside of the tube. Reach in through
the driver opening to do this.
- Lastly.
- Vaccum
out the interior in case there's debris still hiding
in there.
- Mount
driver to the baffle. The supplied gasket is pretty
useless so use rope caulk. Connect the wiring, then
screw the driver down.
- Retraced
steps.
- As
noted in the results section below, there was
excessive vibration on the tube and top endcap. I decided
to take the tube assembly apart and try and damp out
the vibration without having to rebuild the endcaps.
I added a layer of 6 lb carpet padding to the inside
surface of the tube. This was glued in place.
- The
tube was then glued to the endcaps with Liquid Nails
construction adhesive.
Building
the Amplifier
There wasn't
much to do on the Parapix amplifier. The modules arrived almost
ready to use. Here's what I did :
- Modifications
to the amplifier.
- The
best place to obtain infomation on the Parapix amp is
on the Apex
Jr. web page.
- I
used a 48 VCT 3 Amp transformer, which mounted directly
to the component side of the Parapix faceplate on two
of the existing mouting holes.
- For
the power wiring harness, I connected five of the six
wires (two for the primary, three for the seconday of
the transformer). I decided not to wire pin 1.
- The
amp jumper is set to bridge mode.
- Since
the amp is external to the subwoofer, I needed two connectors
for the amp's output. I mounted a pair of 5-way binding
posts from Radio
Shack to the faceplate where the Paramount logo
sits. I spaced them 3/4 inch apart for use with standard
dual plugs.
- Next
to the Peak LED (between the two knobs), I drilled
a 1/4 inch hole and mounted a plastic T1-3/4 LED retainer
to hold the Power LED.
- Next
to the LEDs, I mounted a SPDT switch. Three wires from
the switch were connected to a pair of headers salvaged
from the original metal housing (see below). These headers
go to the three pins of the boost circuitry. This allows
the user to enable or disable the boost rather than
hiding this feature on the amplifier PCB. Make sure
to mount the boost switch to make sense - up for boost
on, down for boost off.
[Added
boost switch with wiring headers and power LED; 10,296
bytes]
- Housing
for the amplifier.
- The
metal casing is from an old Exabyte 8 mm tape drive
whose mechanisms have long ago seen the local land fill.
The only parts I kept were the 3 sided metal casing
and some wiring (see above).
[Exabyte
case; 4,786 bytes]
- For
the two ends, I milled endcaps much like the subwoofer
(of course !). Each endcap has a solid cherry outer
piece and a smaller particle board inner piece. The
inner piece is screwed to the outer cap and also to
the metal casing.
- The
amplifier module is mouted to the inner particle board
pieces with screws.
- Black
spray paint and a clearcoat was applied to the metal
casing to match the black Parapix faceplate. The cherry
endcaps received a coating of Danish oil and wax; same
as the subwoofer.
[Metal
box spray painted black, with cherry endcaps; 6,850
bytes]
Results
To test
the subwoofer, I used the line level output of my PC sound
card (Turtle Beach Malibu)
to drive a Rotel amplifier. Later I repeated this test with
the Parapix amp. This particular sound card has decent low
end extension (see test results at the PC
AV Tech web site) so I wasn't worried that it would limit
the low end test signal.
When I cranked
the volume up, I noticed that the tube wall and top endcap
vibrated. This should not happen with a tubular enclosure.
Adding mass to the top decreased the vibration; sitting on
it removed all of it. I concluded that I did not do an adequate
job of strengthening the top endcap - there was no bracing,
the inner circle was low grade plywood, and as mentioned previously,
I had neglected to fill the void where the nuts are hidden.
I tried
to do what I could short of ripping things apart. I glued
the tube to the endcaps, and added carpet padding to the tube
walls. This seemed to help a wee bit, but the walls still
vibrated. The real solution was to rebuild the endcap. Since
I didn't have the time to do this, I decided to place the
subwoofer into service and worry about it some other time
- hey, this is DIY, which means things are never really done
!
No measurements
were ever made. Instead I simply listened, looked,and felt
the results. It was pretty obvious that the frequency response
cutoff was in the mid to upper 20's as predicted. As for SPL,
it can definitely crank but it didn't take much to reach the
driver's excursion limit. Nonetheless, the SPL at that point
is more than enough for HT use in a "typical" room.
29-September-2000
|
|
(4)
[page
1][page 2][page
3]
|
Note: The
contents in these pages are provided without any guarantee,
written or implied. Readers are free to use them at their
own risk, for personal use only. No commercial use is allowed
without prior written consent from the author.
|
|